| The Genset Saga |
|
The morning before I planned to leave Marsh Harbor
I started the generator as normal to re-charge the batteries and
draw down the frig and freezer.
No more than 5 minutes after the generator started it shut
down. This had never
happened before. I
guessed that it might be an over temp condition.
Normally this was preceded by an alarm, but since the hour
meter was no longer working it was possible the alarm was not
working as well.
I waited an hour or so, and then started the
generator again. This
time I checked for water flow out of the exhaust.
There was none, so I quickly shut down the generator.
While sorting this problem out I used the main
engine to charge the batteries and run the refrigeration compressor.
|
|
The most likely culprit for no water flow is
the impeller in the raw water pump.
I’d never changed this impeller since I purchased Sarah with
the generator installed.
As a matter of fact I didn’t even know where the raw water
pump was located on the engine.
So I got out the parts catalogue for the generator and
located the pump.
Surprisingly it was fairly accessible on the forward, port side of
the engine. I was able
to remove the pump cover from the cockpit reaching through the aft
lazarette. The four
small machine screws that held the cover on the pump all came of
with minimum effort.
Maybe this was not going to be such a bad project after all.
Well
I could not remove the impeller from the cockpit, so I emptied the
contents of the port cockpit locker and climbed in.
By squeezing myself (no small task) around the propane locker
I could see the pump.
The picture on the left is my view of the pump.
In this picture the impeller has been removed.
In order to remove the impeller I had to get two prying
devices (aka screw drivers) into opposite sides of the impeller and
pry it out. This was
very difficult as the propane locker was in the way.
I was just able to get one arm on each side of the locker and
get two screw drivers into the pump housing.
It took several tries, but finally the impeller came free.
The
picture on the right shows the removed impeller.
I think I got my 25¢ worth out of this sucker.
I have no idea when that impeller was installed.
Suspect it was the original impeller in the generator when it
was installed, nearly 20 years ago.
All missing vanes on the impeller are a worry.
They were not in the pump housing when I removed the
impeller, so they are either in the hoses or the heat exchanger. |
| Missing
Impeller Kits |
|
First I have to get my hands on one of the
spare impeller kits I have onboard.
My first step was to start up my
Inventory application on the PC and search for them – Not
Found!. The inventory
finds the impellers for the Yanmar engine, but not the Northern
Lights generator. After
trying several search options I gave up – I must not have
inventoried those impellers, but I know I have them onboard.
I then resorted to the brute force search
method. I opened each
locker in the aft cabin and removed every item looking for those
impellers – Still Not Found.
|
|
Finally it dawned on my.
Prior to starting the Yanmar installation I removed all of
the contents of the aft cabin lockers and the cockpit lockers.
I put much of the stuff in the dockhouse at the marina, but
some of the stuff went in the trunk of the car.
After the Yanmar installation was complete, I moved the stuff
in the dock house back onboard.
It appears the stuff in the trunk of my car is still there –
in Lexington Park,
MD.
So now the task is to find a dealer who can
provide the impeller kit.
From the Northern Lights website I found 2 dealers in The
Bahamas, both in Nassau.
I could have gone to a dealer in
Florida
to order them, but then I would have to deal with Bahamian Customs
on my own. I decided to
place the order with Marine Diesel Ltd.
They did not have the part,
but they did order it for my through the Northern Lights distributor
in Florida.
Almost immediately I got a call back saying that Northern
Lights says the part number I gave them was obsolete and no longer
orderable. I thought it
strange that they would not just provide the superseding part
number. I got my part
number from the catalogue for my generator.
I went to the Northern Lights website and downloaded the
latest parts catalogue for this generator.
There I discovered new parts numbers for the water pump and I
called them into Marine Diesel Ltd.
That seemed to take care of the problem and I was assured my
parts would arrive in 3 days, which they did.
Then I discovered the danger of not reading the
parts catalogue carefully.
Those part numbers were for a different pump.
My old pump had been discontinued for a number of years and
the impeller kits were no longer available, at least not from
Northern Lights. The
only option now was to order a complete replacement pump – another 3
days.
|
| New Water Pump |
|
Finally
on Saturday, Jan 17 I had the new pump on board.
The first thing I noticed was that
an O-Ring is required on the pump mounting.
No O-Ring was supplied with the pump.
This appears to be just a 1.5”x1/8” O-Ring so maybe I can get
one from a local HW store.
In the meantime I need to get busy removing the old pump.
I waited to remove the old pump until after the
new one arrived so I had something to refer to other than the parts
diagrams. Looking at
the old pump and the diagrams I found it difficult to visualize how
it was mounted. The new
pump helped me understand those diagrams.
|
|
Looking at the pump mounting base in the
picture above, you can see there are holes for four mounting screws;
however, two of the holes are threaded.
So 2 of the screws are threaded onto the gear housing on the
engine and the other two threaded from the gear housing into the
pump mounting flange.
Also the shaft that protrudes from the mounting end of the pump
secures to something inside the gear housing.
At this time I did not understand how this pump connected to what I
assumed were gears inside the housing on which it is attached.
Once more the drawings provided by Northern Lights were of no use.
|
| Removing the
Old Pump |
|
Having
determined how the pump is mounted I started to assemble the tools
necessary to remove the old one.
The parts diagrams did inform me that the mounting screws are
M8 cap screws. One is
110mm long, the other three are 60 mm long.
The head of the 110mm screw is shown in the picture on the
right. This longer
screw goes the entire length of the gear housing.
The threaded end of one of the 60mm screws are visible on the
right side of the picture.
|
|
The
picture on the left shows the 60mm screw, which threads into the
pump mount flange. As
you can see getting a wrench on these screws is not going to be
easy, especially since I cannot see these screw heads. I took
these pictures by blindly aiming the camera. I had to take
dozens of pictures to get a few that told me where the screws were
located.
|
|
The
easiest screw heads to reach appear to be the ones that thread into
the gear housing, so I decided to start there.
First I removed the water hoses from the pump.
When I did I discovered
where most of the impeller vanes went – into the feed hose which
attaches to the bottom port on the pump.
Before I got too far I quickly discovered that
I do not have an open wrench that will fit the heads of these
screws. The heads are
13mm Hex. I have 12mm
and 15mm open wrenches but nothing in between.
That is not totally correct I do have a 13mm open wrench that
came with the Yanmar engine, but these wrenches are pretty
worthless. They have
very thin faces, and do not get a really good grip on the screw
head. I would be
concerned about rounding off the heads with this cheap wrench.
If possible, I wanted to use a box wrench on these screws to prevent
rounding the heads.
So it was back to the HW store on the next day
(Monday) to get another wrench.
I also picked up the O-Ring as well as replacement screws
(incase I mess one or more of them up).
Then work stopped for a couple of days.
We had a series of cold fronts come through the Abacos on
Tuesday and Wednesday, 1/19-20/2008.
They brought a fair amount of rain and strong winds (20-25
kts) for most of those two days.
I decided to not work on this pump while the boat was
bouncing and rain showers were passing through.
|
|
So on Thursday I finally started to remove the
old pump. It wasn’t
that difficult, just awkward and slow.
I was able to get a socket on three of the machine screws
that held the pump to the gear housing, but the third (naturally the
longest) was the most difficult.
This is the 110mm screw.
There was just barely enough room to get the 13 mm box wrench
on the head, and then there was only enough room to turn the screw
one point before having to re-position the wrench.
That
screw will not come completely out of the gear housing, but with it
loose I could pull the old water pump off the housing.
In the picture on the left the old pump and the new one are
side by side.
Now I understood how the pump was driven.
There is a gear on the shaft of the old pump.
The gear is seated firmly on a tapered shaft.
I do not want to try to pry it off the old shaft as that
would likely damage the gear and the old pump.
I want to keep the old pump in my parts bin as a backup or I
will sell it on eBay – that is assuming those old impellers are
still in the trunk of my car and they are serviceable. So I
now need a gear puller. One more trip to the Marsh Harbor HW
and automotive stores produced nothing satisfactory. Finally I
called the Marsh Harbor Boatyards and arranged for their machinist
or mechanic to remove the gear from the old pump and put it on the
shaft of the new one.
|
|
When
I removed the old pump I found more impeller vane debris in the
intake port of the pump.
It is amazing how long that damaged impeller was still able
to pump water through the heat exchanger.
I believe that impeller was in bad shape when I bought Sarah
in 2000. It never put
out much water through the exhaust, but I had never seen the normal
water flow for comparison.
I put several hundred hours on the generator with that water
flow. It will be
interesting to see what the flow will be like with the new pump and
an intact impeller.
|
| Installing
the New Pump |
|
Before
installing the new pump I took a picture of the pump housing to
insure I understood how the pump would fit.
In the picture on the left you can see the gear that engages
the pump protruding into the right side of the housing.
|
|
Mounting
the pump was fairly straightforward at first.
I was getting pretty good at working those largely
inaccessible machine screws.
However once the pump was mounted I had a problem connecting
the output hose going to the head exchanger.
As you can see in the picture on the right the hose barb on
the pump is very close to the engine.
So close I could not get the hose onto the barb.
The hose barb has a small flange that increased the outside
dimension of the barb by about 1/8”.
My only choice was to remove the pump and file
down that flange. So I
got a little more practice on those inaccessible screws.
After the 30 minutes of filing the hoses would once more fit
on the pump. I decided
to attach the output hose before mounting the pump.
There still wasn’t very much room between the barb and the
engine.
|
|
After
another struggle with the screws the pump was mounted and the hoses
connected. Now I was
ready to test generator.
I opened the seawater valve for the generator
and hit the starter.
The generator came to life quickly and I checked over the stern to
see more water coming out of the exhaust than I’ve seen in my
ownership of Sarah.
Clearly the impeller was failing when I purchased this boat.
It is amazing that it continued to work for the past 8 years.
That is probably a testament to how Northern Lights may have
over-engineered the cooling system, but also to the fact that I’ve
never really put a heavy load on this generator.
|
| Now For
the Next Problem |
|
Well
I was ready to declare victory, put my tools away, and plan for an
early departure from
Marsh
Harbor in the morning.
Then I looked down into the locker where the generator is
installed.
Not only was the generator putting a lot of
water out the exhaust, it was also putting a lot of water into the
boat. Sea water was
streaming out of the water lift muffler.
The end plate on the muffler had finally corroded through.
I think it had been leaking slightly for some time.
You can see the accumulation of salt next to the trap.
Now I was back to a non-working generator and
the need for a part I can’t find locally.
I was totally bummed from a 3 week ordeal of getting parts
and now back to the beginning.
|
|
After one night of feeling sorry for myself
(and doing major damage to the liquor locker) I once more contacted
the Marsh Harbor Boatyard to order a replacement water lift muffler
and to get back on the mechanic’s schedule.
The muffler was immediately ordered, but the mechanic was not
available until Feb 10, more than a week away.
I spent a couple of days trying to get the old
muffer removed. I
really wasn’t trying very hard, I had pretty much resigned to
sticking in Marsh Harbor
until the 10th and then let the mechanic do the job.
So
finally on the morning of the 10th I pulled up the anchor
for the first time in over a month and motored around Mat Lowes Cay
to the boat yard on the other side of Marsh Harbor.
Within a few hours the mechanic had the old
muffler out and the new one in place (picture on the left).
I started the generator and it came to life and kept running.
We had excellent water flow and 120 volts on the power panel.
Everything looked good.
The mechanic hung around to tighten the stuffing box on the
rudder (the bilge pump was coming on twice a day for about 20
seconds), and did a quick review of the main engine installation
(he’s a Yanmar guy). It
was nearly lunch time so the mechanic left and I started
straightening up the boat.
|
|
Finally, I
Discover the Original Problem |
|
I decided to run the generator all afternoon to
be sure it was working properly.
When I restarted the genset I realized that I had all the
power loads turned off when we ran the generator earlier.
When I turned on a few loads the genset engine stalled.
After that I could start it, but it would quickly stop.
This was pretty much the symptom I had when I started on this
voyage of discovery.
Now I was certain this was a fuel problem.
I was also fairly certain this was the original problem, not
the lack of seawater flow through the heat exchanger.
All those water pump/muffler problems were real and needed to
be fixed, but the basic problem that caused the genset to shut down
had not been addressed.
The first thing I checked was the primary fuel
filter. It was a little
dirty, but nothing severe.
I replaced it with a new cartridge just to be sure.
When I restarted the genset it still stalled and shut down
under load.
Next I attempted to bleed the fuel lines.
The owner’s manual provides no guidance on how to do this.
On engines I previously owned the bleed valve was on top of
the secondary fuel filter.
I loosened the bolt and manually operated the lift pump and
got clean fuel out of the valve.
I closed the valve and once more started the engine – same
problem.
Although I was still convinced this was a fuel
problem, I was stumped.
I had done all the things I knew to do.
I had already gone to the yard office and requested the
mechanic return to help me with the problem.
He had gone to another job and it was a couple of hours
before he returned.
The
first thing he pointed out was that there was another bleed valve on
the fuel line going into the injector pump.
When he bled that valve he got lots of air bubbles until the
fuel started to run solidly.
We restarted the genset, but it immediately shut down.
The mechanic opened the bleed valve once more and once again
got air bubbles in the fuel lines.
Still the genset would not stay running
We repeated the bleeding several more times
until there were no bubbles when the valve was opened.
Finally we were able to start the genset and it stayed
running under full load.
I stayed at the boat yard that afternoon and evening and ran
the genset repeatedly for several hours each time.
The problem appears solved, for now.
What I don’t understand is how the air got into the fuel
lines initially. So I’m
not fully convinced the problem won’t return sometime in the next
few days or weeks.
However, for now I have a working genset and
the Bahamas cruise
will continue after being on hold for a month.
|
| The Saga Resumes |
After
over a month of flawlessly working, the generator failed once more.
One evening in mid-March, I started the generator and immediately
noticed that the output voltage was about 6 VAC. I shut down
the generator, turned off all circuits and started it once more.
My electrical panel still read only 6 VAC. I shut it down
again and ran the engine that night to charge the batteries and run
the frig. The next morning I tried the generator again and
still got only 6 VAC on the meter. I opened the junction box
on the generator (picture on the left), which contains all of the
electrical wire connections. I checked the output of the
generator with a multi-meter - again only 6 VAC. |
After
studying the operator's manual and the parts diagram, I decided to
just order the Automatic Voltage Regulator (AVR) from my new best
friends in Nassau. The existing AVR is shown in the picture on
the right. I reasoned that this problem was likely electrical
and not mechanical. A broken wire was a possibility, but I
reasoned that broken wire the output would be 0 VAC not 6 VAC.
Also I could find no wire breaks, at least not in the wires that I
had access to. The other electrical components that might
cause this problem are the brushes, the rotor and the stator.
I couldn't deal with a rotor or stator problem and I knew getting
access to the brushes would be very difficult, so by means of
eliminating the problem sources I didn't want to deal with, I
ordered a new AVR. |
The
new AVR arrived in about a week (picture on the left) and it was
easy to install. I quickly started the generator and once more
saw 6 VAC on the electrical panel. Nuts! Now I was going
to have to deal with those parts of the generator that I didn't want
anything to do with. |
When
all else fails RTFM (Read the F_____ Manual). Buried in the
operators manual were specs on the ohm meter readings I should get
from the three wires connected to the AVR. Two of
the wires checked in specs, the wires going to the brushes showed
infinite resistance (open circuit), which should have been around 17
ohms. The problem must be either in the brushes, the rotor or
stator. Again using my preferred methodology of avoiding the
least desirable sources of the problem, I placed an order for a new
set of brushes.
The picture on the right shows the existing brush assembly after I
removed the cover plate on the generator. I removed the
machine screws that held the cover plate in place without ever
seeing them - the usual Braile boat maintenance process. I
took this picture by blindly aiming my camera at this part of the
generator that I can't see from the aft lazarette. To get at
the brushes I'll have to get into the starboard cockpit locker - a
very difficult fit for me. |
This
is another blind picture of one of the rotor coils and a portion of
the stator. You can probably guess why I really don't want
either of these to be the problem. |
When
I received the new brushes I started to look seriously at how I
would install them. This is the view from the starboard
locker. What I quickly learned was that the recently installed
waterlift muffler blocked access to the brushes from this location.
So to do the install from this locker the first thing I had to do
was remove the muffler and exhaust hose.
Since I really can't fit in this locker and do any work, I decided
to bag the generator problem for now. This problem will have
to wait until I get to a boatyard with the necessary Munchkin who
can work in this restricted space. Then I'll likely find the
problem is not the brushes. I can only guess what a new rotor
or stator costs, or how they could be installed without removing the
entire generator.
In the mean time the Bahamas cruise continues without a generator. |
| Back In
Operation (Again) |
Upon returning to the USA in early May I took a berth at the
Cape Marina in Port Canaveral, FL. I needed to rest after the
24 hour run from Great Sale Cay, but also I wanted to have a
technician look at the generator and tell me what needs to be fixed.
Cape Marina is the NL dealer for the area, so I figured their
technicians should be able to work on the problem. Therefore I
reserved a berth for a week, knowing nothing happens tomorrow in a
boatyard.
I filled out a work order for the generator and the next day met the
yard manager. He immediately recommended I turn the job over
to MarinePro in Cocoa, FL Turns out MarinePro is the leading
Yanmar and Northern Lights service company for the Space Coast of
Florida if not the entire SE. I felt confident turning the job
over to them, but the only problem was fitting into their schedule.
When you're the best you generally have a lot of work. After 3
days and a weekend I still wasn't on their schedule. I really
didn't want to leave Port Canaveral without coming to some
resolution on the generator. I felt once I left it would be a
long time before I had access to qualified service personnel.
So
I persisted in calling MarinePro each day to check on the status of
my work order. Finally the day before I planned to depart Port
Canaveral I got a call from MarinePro that one of their guys would
be here that afternoon, and around 2:00 PM he showed up and went to
work.
My biggest concern was that the problem was in the Rotor, which I
knew might be prohibitively expensive to replace. My hope was
that the Brush Assembly I purchased in the Bahamas would fix the
problem.
Very quickly the mechanic determined the problem was indeed the
brushes. When he removed the brush assembly one of the carbon
brushes all but disintegrated in this hand (photo on left).
Since I had the spare Brush Assembly on board, he took only a few
minutes to install the new brushes. I started the generator
and once again saw 125 VAC on the electric panel. |