| Installing a New Galley Faucet |
| In the middle of a large number of upgrade projects on Sarah
during the spring of 2008, the six year old galley faucet decided
it was time to spring a leak.
So I purchased a much more pricey Price-Pfister faucet and expected to get this job done in a single afternoon. Replacing a faucet on Sarah should not be a major project. Most of us have done this in our homes many times, and the job is not that dis-similar on a boat. However this is boat plumbing, not home plumbing, nothing is straight-forward with boat plumbing. When I installed existing faucet (picture on the left) I was able to tighten the main nut under the sink counter with a standard basin wrench. This time when I slid on my back under the sink I could not loosen the nut with the same basin wrench. |
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This wasn't a big job, but it did require more working on my back unscrewing the 6 sink clips that held the sink in place. |
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Four of the six clips were in good condition. Two were somewhat corroded (as shown in this picture) and required a little gentle persuasion to release the sink from the counter. I wanted to replace the corroded clips before re-installing the sink, but neither Loew's nor Tru-Value (only hardware stores in my area) carry this type of clip. So I'll just soak them in a little CRC until the sink is ready to go back in. |
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I've forgotten how the original faucet was connected, but I had to use a pair of 5/8"to1/2" male-male thread adapters on the compression fitting so I could use a standard faucet 1/2" connector hose for the faucet I installed in 2001. I had hoped to change this arrangement as the shortest hookup hoses available in hardware stores are about 3x the length required. I would also like to put shut-off valves on each of the water hoses so that the galley faucet could be removed and serviced without have to de-pressurize the entire freshwater system on Sarah. However, since I was trying to get this job done in a single afternoon I decided to just replace the faucet hookup hoses in kind. |
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I remember this from my earlier installation, but at that time I just fitted the new faucet in the hole and tried to secure it with the faucet nut and washer. This worked, but the faucet did wobble a bit. I also didn't put any plumber's putty under the faucet base so water seeped under the base. For this installation I cut a piece of cleat stock wood with the correct size hole to use as a backing plate under the sink. I also sealed the new faucet plate with plumber's putty. |
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| New Faucet Installed, but Old Problem Didn't Go Away |
| The leak was the reason I decided to replace the old faucet now
rather than later, but that wasn't the real pressure water problem I
was fighting this spring. Actually the problems started nearly
a year ago. Shortly after we departed Madeira on the way back to the states I started to have problems with the pressure water system. The symptom has always been air in the system. Initially this problem was limited to a single tank (Starboard). I switched it to the bow tank gate valve on the manifold and the pump primed to full pressure. I replaced the gate valve when we got to Bermuda and everything was fine for a few months. Then the problem with the Starboard tank returned. This time I replaced the entire manifold using ball valves instead of gate valves. That also seemed to fix the problem, but shortly thereafter the pump starting sucking air again, but now from all tanks. Eventually I determined that the water strainer I added to the manifold was the source of the leak. I removed the strainer and I thought now I could forget about the pressure water system for awhile and get on with my other projects. Now after installing the new faucet, the pump still won't shut down and one of the connections for the new faucet is leaking. Suddenly I realized that this was a new problem - the pressure sensor on the pump must have failed. So I installed my backup pump and the system pressurized normally - or at least what was normal almost a year ago. So the faucet leak was most likely due to the pump over-pressurizing the system. I may have been lucky none of the 30-year old polyethylene hoses didn't burst. That would have been a real project. |
| I'll run this system for a few days before I finish re-installing the sink just to be sure. I have a third pump onboard for spare parts. I believe the motor on that pump is burned out. I had planned to see if I could find a cheap motor that would drive this pump as an emergency backup. Now I'll see if the pressure switch on that pump will fix the pump I just de-installed, then disassemble the rest of the pump into my parts bin and throw away the bad motor. |
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Well after a few hours of operation on my backup pump, another old problem is back - air in the lines. The symptom is that the pump cycles a few times every 15 - 30 seconds. This, I believe, is due to air in the lines or in the pump. This was the very symptom that got me to switch pumps after I installed the new tank manifold. I've changed so many things in this system it is difficult to document what was happening when, but I did not have this pump "creep" with the pump I just replaced because of the faulty pressure sensor. So I think the "creep" problem must be in this backup pump. So now I have 3 of these expensive pumps and all of them have at least one problem: |
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| Hopefully I can use the parts from these three pumps to make one working pump. However I plan to buy another pump as my primary. I believe the Jabsco Max 4 pump uses the same hose connectors has the Sensor Max VSD, so it should be a drop-in replacement for these VSD pumps. I've lost all confidence in these fancy new pumps and will go with the cheaper, more reliable (hopefully) technology. The VSD pump will just be a temporary backup in case of primary pump failure. |
| Well, at least now I can put the sink back in permanently. |
| Another New Pump |
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The picture on the right shows the new pump installed (looks familiar, huh?). |
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With that I re-secured the sink after running a bead of Plumbers Putty all around under the sink flange. Once more on my back to install the sink clips, and the installation was done. Another few minutes of cleaning up the mess on the counter and putting all the cleaning stuff back under the sink and I could take the pictures on the right and below. |
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| Problems Solved - NOT! |
| Clearly the pump I replaced was defective and the new pump
solved at least one of my problems. However after a few days
of operation I was back to the old problem of the pump not being
able to draw water from the Starboard tank. I switched to the
Port tank while I tried to figure out where I go from here, but the
pump could not draw from that tank as well. So I was back to
square one and completely baffled. When I disconnected the
hoses from the tanks from the manifold, water flowed freely, so the
problem had to be in the manifold or the pump. I had no
intention of buying another pump, so I was on the verge of ripping
out the manifold and replacing the whole thing with PVC components
as other 424 owners have done. Before heading off to Loew's once again, I tested the manifold by blowing into connections to the tank hoses. This is something I had done every time I re-installed the manifold to insure there was no blockage in the valves or tubing. This time I could blow very little air from any of the hose connections through the manifold. Clearly there was some sort of blockage. By manipulating the valves I determined that the blockage had to be in the upper part of the manifold - an elbow that connected to the hose going to the pump. So once more I took the manifold to the marina workshop and disassembled the upper part. Inside the elbow I discovered a small self-tapping screw! With the screw removed and manifold reassembled, the blockage was removed. I re-installed the manifold and the pump drew water from all tanks. After another 2 weeks of operation I am finally convinced that my freshwater system is back to normal. The only question is how did that screw get into the manifold. I know there was no blockage in the manifold the previous time I re-installed it. My only guess is that one of the times I removed the manifold, one of the screw that I used to hold it to the bulkhead may have dropped into one of the delivery hoses from the tanks (mostly likely the starboard tank). Those hoses stand vertical on the bulkhead. The hoses are old vinyl and nearly opaque so I would not have noticed the screw if were inside the hose. I do vaguely remember not being able to find one of the screws during one of the re-installations. Later when I re-installed the manifold and started the pump, the screw could have been sucked up into the tubing. That would explain why the problem was mostly with the Starboard tank. Eventually the screw could have worked it's way through the manifold to the top elbow, where it was lodged. It is possible that sometimes it was lodged sideways in the tubing and only partially blocking water flow. Whenever I de-pressurized the system when I was fooling with the pumps and then re-pressurized the orientation of the screw in the tubing could have changed. That would explain why it always initially appeared that my changes to the system had fixed the problem. After a few dozen pump cycles that screw may have re-oriented itself to effectively block the water flow. No matter how that screw got there (it might have fallen into one of the tanks and been sucked through the hoses) I think things are working again. I do need to add a filter in the hose going to the pump. I threw away the one I originally installed thinking it was defective. I have another, but I think I'll enjoy a few more weeks of flawless operation before I make any more changes to this system. |