Engine Work
Click on picture to view at full resolutionAlthough not really upgrades, during the first year I owned Sarah I had to have a great deal of work done on the engine.  Some of this was detected by the pre-purchase survey, but the need for most of the work was not apparent until I had put a few more hours on the engine.  This work included the following:
  • Heat exchanger cleaning
  • New engine mounts
  • V-Drive re-build

In preparation for the Bermuda cruise, I replaced all of the water and exhaust hoses on the engine.

  

Click on picture to view at full resolutionOn the left is the original, 30-year old Westerbecke 60 Engine.  Other than having to replace a few very expensive parts (heat exchanger, fresh water pump, etc.) this engine has served me very well.  I've put several thousand hours on the engine since I purchased Sarah in 2000, including one summer of almost continuous motoring in the Mediterranean Sea.

Finally after returning to the USA in 2007 it was time to retire this workhorse. 

In January, 2008 I moved Sarah to Zahniser's Yachting Center and started the process of replacing the engine and the fuel tank.

I have set up a separate page to cover the details of this repower.

The picture on the left was taken a few hours before the Westerbecke was removed from Sarah.

 

High Volume Sea  Water Intake Manifold
When I purchased Sarah she was equipped with both a Westerbecke 60 diesel engine as well as a Northern Lights diClick on picture to view at full resolutionesel generator.  Both engines were cooled by seawater from separate 1" seacocks and through hulls.  Both systems required separate raw water strainers to prevent debris from getting into the seawater pumps.  The seacocks were actually just ball valves screwed into the through hulls, which does not provide much support against a shear force.  These valves did not appear to be high quality and showed signs of corrosion.  Since I needed to replace those valves, I decided to reduce the number of through hulls by combining the two seawater circuits into one 1 1/2" seacock.  The result is the seawater manifold shown on the right.  The intake seacock is forward of this cabin sole hatch.  The black water hose on the upper right connects the seacock and the raw water strainer.  The manifold, on the left of the strainer, consists of a 1 1/2" "T" fitting connected to two 1" ball valves.  The engine seawater is controlled by the valve on the extreme left of the hatch.  The inboard valve serves the generator.

Therefore although both engines are served by a single through hull, they can be run concurrently and their seawater coolant can be independently shut off and turned on.

For more details on this upgrade see the Haul Out Tasks page.

 

Low Volume Sea Water Intake Manifold
IClick on picture to view at full resolutionn 2000 I replaced three individual through hulls and seacocks with a single through hull and seacock connected to a manifold that delivered low volume seawater to the head, galley sink, refrigeration and air conditioner.  I was not satisfied with this location of the manifold as it intrudes into the hatch space too much.  I decided to move it so that it is more flush with the edge of the floor board hatch.  I also wanted to add a raw water strainer for this manifold.
Click on picture to view at full resolutionOn the right is the modified low volume manifold.  The electric pumps for the refrigeration, air conditioner and shower drain are in the center and the Y-valve for the head discharge is at the bottom of the cabin sole hatch.  You can see bilge pump and float switch at the bottom of the very deep (4') sump.  See the Haul Out Tasks page for the trial and tribulations of this plumbing change.

 

Maxprop Propeller
Click on picture to view at full resolutionThe original propeller on Sarah was a fixed 3-blade 20x10 propeller.  This propeller had a lot of dinks and was showing its 20+ years of age.  It also free-wheeled under sail whenever boat speed exceeded 4 kts.  That put some extra of wear and tear on the transmission and V-Drive.  This probably would not be significant for weekend sailing on the Chesapeake Bay, but for the extended off-shore voyages I have planned it could be problem.  Therefore I replaced this prop with a 20" Maxprop.  The alternative was to install a shaft lock to prevent the propeller from free-wheeling.  The Maxprop does not work quite as well as I hoped in this regard, as the blades tend not to feather when I shut down the engine and start sailing.  If I shut down the engine with the transmission in gear it will normally feather the blades and prevent free-wheeling.  Reverse power with this prop is much more predictable for maneuvering around the dock.   

 

Rudder Stuffing Box
Click on picture to view at full resolutionAs long as I've owned Sarah she has had a wet bilge.  In that time I've tried to find the source of the leak or leaks in vain.  The leaks were so slight I could find no evidence of where the water was coming from.  The leaks were slight enough that I rarely noticed the bilge pump coming on, but no matter how dry I pumped the bilge within a week it would be completely wet again.

I thought I could detect a leak from the propeller shaft stuffing box and I replaced that with a PSS shaft seal.  A marine surveyor who had done work on the boat for the previous owner thought it was possible that a boat yard may have set the boat down on the aft portion of the keel, which is hollow.  He thought the fiberglass may have cracked enough to allow in a small trickle of water.  Before I left for Florida in 2004 I had the lower portion of the keel re-glassed.

All to no avail.  The bilge constantly had an inch or less of water in it.  While living on board in Florida over the winter of 2004-2005 I began to notice that the bilge pump came on at least once every two or three days.  This was more often than I had noticed in the past.  It would come on even more often during rainy weather, which told me at least one of the leaks was on deck.

While sailing across the Atlantic to Portugal I noticed that the frequency of bilge pump activity was increasing.  By the time we were approaching the coast of Portugal the pump was coming on every 2 - 3 hours.  During this period we had no rain.

 
Click on picture to view at full resolutionNow at least the flow of water was sufficient to leave evidence.  I could see a very slight leak coming from under the engine pan.  This meant the leak was coming from somewhere under the cockpit.  That left the rudder stuffing box as the prime suspect.

I could not verify that the stuffing box was leaking because I could not see it.  When originally built this Pearson 424 provided adequate, if not comfortable, access to this stuffing box.  However, the primary access was through the stern lazzarette, which on Sarah houses the generator installed by the previous owner.  The P.O. as installed a small battery box in the port sail locker, which blocked access from that locker.  In the first year of my ownership I installed the drive unit for the autopilot in the starboard sail locker.  So all of the normal access points for the stuffing box are blocked on Sarah.

Once secured in the marina in Cascais, PT the leak reduced to the same amount of bilge pump activity as the previous winter in Florida.  So it was obvious that the leak was greater when Sarah was underway - further pointing to the rudder stuffing box.

 
Click on picture to view at full resolutionOver that winter I started planning how I could get at the stuffing box to either tighten or re-pack it.  The solution arrived in the person of my wee welsh friend, Martin.  Martin could fit down into the lockers in a way I never will and at least he could see the stuffing box.  He confirmed that it was indeed leaking and that there were ample threads on the fitting to allow it to be tightened significantly.  So we probably didn't have to re-pack it at this time.

About this time I was able to get my digital camera down into the area of the stuffing box and took the two pictures above, right and left.  In the top picture you can see the amount of thread below the lock nut (bottom nut).   The picture below on the left shows the moisture on the top of the stuffing box.  This was at least one source the bilge water on Sarah.

Our first problem was to find a wrench of sufficient size to work the nuts on the stuffing box.  We measured the nut with a micrometer to be about 2-1/2".  I have a Channel Locks adjustable wrench that is large enough.  However that type of wrench would be difficult if not impossible to use on the nut.  Through one of the service shops at the marina I acquired a large pipe wrench, shown in the picture on the right.

 
Click on picture to view at full resolutionEven with that wrench and Martin's small size it was still not possible to effectively work on the stuffing box.  We finally removed the port side pulley for the steering cable and Martin could squeeze in between the rudder stop and the generator battery box to get the wrench on the nuts with some leverage.

 

Click on picture to view at full resolutionThe result is the picture on the right.  The stuffing box has been tightened up about one full turn and fitting cleaned up with a wire brush.  As of now there is no detectable leak through the rudder stuffing box.

If it starts to leak again it will finally be time to repack the fitting.  Hopefully that is a year or two off.

Before departing Lago, PT in the spring of 2007 I had the Sopromar Yard attempt to re-pack this stuffing box (it had begun a slight leak after the Med Cruise in 2006).  They also had great difficulty in getting close enough to the gland to effectively clean out the old packing material.  They removed as much as they could then put in as much fresh packing as would fit.