| Mechanical Upgrades |
| Engine Work |
In preparation for the Bermuda cruise, I replaced all of the water and exhaust hoses on the engine.
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Finally after returning to the USA in 2007 it was time to retire this workhorse. In January, 2008 I moved Sarah to Zahniser's Yachting Center and started the process of replacing the engine and the fuel tank. I have set up a separate page to cover the details of this repower. The picture on the left was taken a few hours before the Westerbecke was removed from Sarah. |
| High Volume Sea Water Intake Manifold |
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When I purchased Sarah she was equipped with both a
Westerbecke 60 diesel engine as well as a Northern Lights di Therefore although both engines are served by a single through hull, they can be run concurrently and their seawater coolant can be independently shut off and turned on. For more details on this upgrade see the Haul Out Tasks page. |
| Low Volume Sea Water Intake Manifold |
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| Maxprop Propeller |
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| Rudder Stuffing Box |
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I thought I could detect a leak from the propeller shaft stuffing box and I replaced that with a PSS shaft seal. A marine surveyor who had done work on the boat for the previous owner thought it was possible that a boat yard may have set the boat down on the aft portion of the keel, which is hollow. He thought the fiberglass may have cracked enough to allow in a small trickle of water. Before I left for Florida in 2004 I had the lower portion of the keel re-glassed. All to no avail. The bilge constantly had an inch or less of water in it. While living on board in Florida over the winter of 2004-2005 I began to notice that the bilge pump came on at least once every two or three days. This was more often than I had noticed in the past. It would come on even more often during rainy weather, which told me at least one of the leaks was on deck. While sailing across the Atlantic to Portugal I noticed that the frequency of bilge pump activity was increasing. By the time we were approaching the coast of Portugal the pump was coming on every 2 - 3 hours. During this period we had no rain. |
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I could not verify that the stuffing box was leaking because I could not see it. When originally built this Pearson 424 provided adequate, if not comfortable, access to this stuffing box. However, the primary access was through the stern lazzarette, which on Sarah houses the generator installed by the previous owner. The P.O. as installed a small battery box in the port sail locker, which blocked access from that locker. In the first year of my ownership I installed the drive unit for the autopilot in the starboard sail locker. So all of the normal access points for the stuffing box are blocked on Sarah. Once secured in the marina in Cascais, PT the leak reduced to the same amount of bilge pump activity as the previous winter in Florida. So it was obvious that the leak was greater when Sarah was underway - further pointing to the rudder stuffing box. |
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About this time I was able to get my digital camera down into the area of the stuffing box and took the two pictures above, right and left. In the top picture you can see the amount of thread below the lock nut (bottom nut). The picture below on the left shows the moisture on the top of the stuffing box. This was at least one source the bilge water on Sarah. Our first problem was to find a wrench of sufficient size to work the nuts on the stuffing box. We measured the nut with a micrometer to be about 2-1/2". I have a Channel Locks adjustable wrench that is large enough. However that type of wrench would be difficult if not impossible to use on the nut. Through one of the service shops at the marina I acquired a large pipe wrench, shown in the picture on the right. |
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If it starts to leak again it will finally be time to repack the fitting. Hopefully that is a year or two off. Before departing Lago, PT in the spring of 2007 I had the Sopromar Yard attempt to re-pack this stuffing box (it had begun a slight leak after the Med Cruise in 2006). They also had great difficulty in getting close enough to the gland to effectively clean out the old packing material. They removed as much as they could then put in as much fresh packing as would fit.
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